hi,
i have built an interface for use with fms and the MC-15 from JR/Graupner. it works. but the throttle elecator and the rudder are a bit "noisy" that means, they are not stable, so it is difficult to fly. especially when i put the elevator down , or the throttle down or rudder left, they always have some peaks. in the other direction eveything is ok. i modified the interface (input) like ken's setup for JR controllers, but it doesnt work. i have the new software from rasmus in an 12c508A, using BC547 and BC557. i think it may be a softwareproblem, the pots from the controller and the cable are good. has anyone a solution or experience with the pic and mc-15?